Swro Design and Energy Recovery Part 3: Major Component Selection

The sand screens and micron filters werewere several reasons the actual value was lower,
selected because of the durable and corrosionthe main reason however, was the conservative
resistant fiberglass and PVC construction. Thedesign. Because of some uncertainty in the feed
specific model of Eden micron filters was chosenwater quality, the SWRO system was designed
to maintain the filter element flux atwith a relatively low flux (approximately 8 gpm
approximately 3.3 gpm/per 10" equivalent.ft2), and a somewhat large hydraulic envelope. As
Due to the relative remoteness of the installationit turned out, the feed water TDS was closer to
site, multistage-centrifugal, high-pressure pumps36,000 ppm and fairly stable. The lower feed TDS
have been selected for their reliability, availabilityenabled the system to operate at a lower
of parts, economics of operation and easymembrane feed pressure of 790 psi and a higher
maintenance. Centrifugal pumps in general arepermeate flow rate of 120,000 gpd, consequently
smoother, quieter, and require less ancillaryusing less energy than originally projected and
equipment (i.e. pulsation dampeners) than positivemaking higher quality permeate.
displacement pumps. Hydropro has found thatConclusion
positive displacement pumps are much moreWith most of the system assembled, the
prone to failure and lengthily downtimes thaninstallation was fairly straightforward and went
high-quality centrifugal pumps.smoothly. The two units were installed, started
The Grundfos Booster Modules were chosen forup, tested and operator training was completed in
several reasons. The inline style helped conserveless than three weeks. There was, however, a
space and provided ease of installation, allowingproblem with the feed water quality and the
everything to be mounted on the same skid (withpretreatment system, which was discovered
the exception of cleaning/flush tanks, raw waterafter only 24 hours of operation. It immediately
booster pumps, and chemical feeds). Thesebecame apparent that the raw water was loaded
submersible, multi-stage centrifugal pumps werewith particulate that was quickly fouling the sand
also chosen because they are very efficient andscreens and the micron filters. Fortunately, the
quiet, and are constructed of corrosion resistant,feed system could be modified to flow into an
904L super austenitic stainless steel.existing 250,000 gallon seawater tank from the
The high pressure feed and concentrate headerswells, and the SWRO feed was then drawn out
were made of 2205 duplex stainless steel forof this tank. This settling tank solution worked
superior corrosion resistance, and the structuralquite well and provided a feed water with a
skid was constructed of FRP for low weight andpre-filter SDI of 1.25.
zero maintenance. ERI´s Pressure ExchangerThere was also one other performance issue that
was chosen because of its high energy efficiency,needed to be resolved. Initially, the permeate
dependability, and corrosion resistant materials.quality was less than what was projected, and it
Performancewas not clear why. The system was extensively
Values for the projected power consumptionchecked ant tested for leaks, and the possibility
rates that were presented in the proposal werethat seawater was somehow mixing with the
based on a 27ºC feed stream of 45,000 mg/lpermeate was eventually eliminated. It was finally
TDS and a permeate flow rate of 100,000 gpd.determined that the membranes did not meet the
The membrane manufactures projectiondesign rejection required to produce the projected
software was used to determine the systempermeate TDS. Once the membranes were
parameters at a recovery of 35%, and thesereplaced, the system was making plenty of high
parameters were subsequently used to determinequality permeate that was well below the
the projected power consumption. The result wasmaximum acceptable permeate TDS.
an anticipated feed pressure of 900 psi and aKAJUR and the residents of Ebye have since
specific power consumption rate of 3.02 kWhbeen enjoying low-cost, high-quality water for
m³.over a year now without any noteworthy
Once the system was installed and operating, thesystem failures. They are so pleased, in fact, that
specific power consumption was calculated basedKAJUR has recently awarded Hydropro another
on actual system parameters and the result wasSWRO job utilizing work exchanger energy
a much lower value of 2.65 kWh/m³. Thererecovery.